nautilus: remove internal pull down on rev0 and rev1.

We don't need internal pull down for GPIO_ACCELGYRO3_INT_L
on rev0 and rev1.

BUG=b:70299498
BRANCH=none
TEST=build/flash nautilus rev1, sensor operates well

Change-Id: I2f5d71fbd35da2eaebd59f5f5d6ef6c410d5e3e3
Signed-off-by: Jongpil Jung <jongpil19.jung@samsung.com>
Reviewed-on: https://chromium-review.googlesource.com/818584
Commit-Ready: Jongpil Jung <jongpil19.jung@samsung.corp-partner.google.com>
Tested-by: Jongpil Jung <jongpil19.jung@samsung.corp-partner.google.com>
Reviewed-by: Philip Chen <philipchen@chromium.org>
Reviewed-by: Shawn N <shawnn@chromium.org>
This commit is contained in:
Jongpil Jung
2017-12-09 11:21:51 +09:00
committed by chrome-bot
parent 8c75d42d42
commit afc15186f8

View File

@@ -434,7 +434,7 @@ static void board_init(void)
/* Level of sensor's I2C and interrupt are 3.3V on proto board */
if(system_get_board_version() < 2) {
/* ACCELGYRO3_INT_L */
gpio_set_flags(GPIO_ACCELGYRO3_INT_L, GPIO_INT_FALLING | GPIO_PULL_DOWN);
gpio_set_flags(GPIO_ACCELGYRO3_INT_L, GPIO_INT_FALLING);
/* I2C3_SCL / I2C3_SDA */
gpio_set_flags(GPIO_I2C3_SCL, GPIO_INPUT);
gpio_set_flags(GPIO_I2C3_SDA, GPIO_INPUT);