mirror of
https://github.com/Telecominfraproject/OpenCellular.git
synced 2026-01-09 17:11:42 +00:00
nautilus: remove internal pull down on rev0 and rev1.
We don't need internal pull down for GPIO_ACCELGYRO3_INT_L on rev0 and rev1. BUG=b:70299498 BRANCH=none TEST=build/flash nautilus rev1, sensor operates well Change-Id: I2f5d71fbd35da2eaebd59f5f5d6ef6c410d5e3e3 Signed-off-by: Jongpil Jung <jongpil19.jung@samsung.com> Reviewed-on: https://chromium-review.googlesource.com/818584 Commit-Ready: Jongpil Jung <jongpil19.jung@samsung.corp-partner.google.com> Tested-by: Jongpil Jung <jongpil19.jung@samsung.corp-partner.google.com> Reviewed-by: Philip Chen <philipchen@chromium.org> Reviewed-by: Shawn N <shawnn@chromium.org>
This commit is contained in:
@@ -434,7 +434,7 @@ static void board_init(void)
|
||||
/* Level of sensor's I2C and interrupt are 3.3V on proto board */
|
||||
if(system_get_board_version() < 2) {
|
||||
/* ACCELGYRO3_INT_L */
|
||||
gpio_set_flags(GPIO_ACCELGYRO3_INT_L, GPIO_INT_FALLING | GPIO_PULL_DOWN);
|
||||
gpio_set_flags(GPIO_ACCELGYRO3_INT_L, GPIO_INT_FALLING);
|
||||
/* I2C3_SCL / I2C3_SDA */
|
||||
gpio_set_flags(GPIO_I2C3_SCL, GPIO_INPUT);
|
||||
gpio_set_flags(GPIO_I2C3_SDA, GPIO_INPUT);
|
||||
|
||||
Reference in New Issue
Block a user