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31fa74cf7d6d40f55bcc54b237e4e47d39024740
There is leakage on SYS_RST_ODL from the internal pullup cr50 has on DIOM0. This change removes the internal pullup on reef. On Kevin there is a bug preventing the EC from being able to pull sys_rst_l up high enoug for cr50 to detect that it is pulled high. This change adds an internal pullup back when cr50 detects that it is on a kevin or gru. BUG=chrome-os-partner:56945 BUG=chrome-os-partner:53544 BRANCH=none TEST=On gru and kevin remove servo verify when apreset is run on the EC it resets cr50 and the AP. Run pinmux and check that there is a pullup on diom0 on kevin but not on gru. Change-Id: Ica4f557745967b93e0bd9c8462916b1f735756ac Signed-off-by: Mary Ruthven <mruthven@chromium.org> Reviewed-on: https://chromium-review.googlesource.com/381322 Reviewed-by: Vadim Bendebury <vbendeb@chromium.org>
For an overview of the Embedded Controller firmware, refer to http://www.chromium.org/chromium-os/2014-firmware-summit For instructions on building from source, refer to http://www.chromium.org/chromium-os/ec-development/getting-started-building-ec-images-quickly
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