Mary Ruthven 31fa74cf7d cr50: remove the pullup on sys_rst on kevin
There is leakage on SYS_RST_ODL from the internal pullup cr50 has on
DIOM0. This change removes the internal pullup on reef.

On Kevin there is a bug preventing the EC from being able to pull
sys_rst_l up high enoug for cr50 to detect that it is pulled high. This
change adds an internal pullup back when cr50 detects that it is on a
kevin or gru.

BUG=chrome-os-partner:56945
BUG=chrome-os-partner:53544
BRANCH=none
TEST=On gru and kevin remove servo verify when apreset is run on the EC
it resets cr50 and the AP. Run pinmux and check that there is a pullup
on diom0 on kevin but not on gru.

Change-Id: Ica4f557745967b93e0bd9c8462916b1f735756ac
Signed-off-by: Mary Ruthven <mruthven@chromium.org>
Reviewed-on: https://chromium-review.googlesource.com/381322
Reviewed-by: Vadim Bendebury <vbendeb@chromium.org>
2016-09-09 17:15:44 -07:00
2016-09-09 12:33:48 -07:00
2016-09-09 17:15:40 -07:00
2016-09-07 14:01:18 -07:00
2016-09-02 21:17:22 -07:00
2012-05-11 09:11:52 -07:00
2016-07-11 21:27:46 -07:00
2014-04-02 19:58:53 +00:00
2015-12-08 20:05:05 -08:00

For an overview of the Embedded Controller firmware, refer to

http://www.chromium.org/chromium-os/2014-firmware-summit

For instructions on building from source, refer to

http://www.chromium.org/chromium-os/ec-development/getting-started-building-ec-images-quickly
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